Set ROP record 38.45 ft/hr and zero NPT
Revolution® Rotary Steerable Systems set field rate of penetration (ROP) record and incurred zero NPT in a field in the United Arab Emirates. The tool enabled the operator to reach TD.
Restored casing integrity in one trip
After previous cement squeeze attempts were unsuccessful at isolating a casing leak, the Weatherford MetalSkin® solid-expandable system delivered complete casing remediation in a single run.
Isolated and fractured 45+ sections in 1 trip
The ZoneSelect® i-ball® stimulation sleeve enabled an operator to fracture 45 individually isolated zones in one trip – without milling or further intervention.
Implemented the 1st complete digital oilfield
Weatherford delivered a complete, automated production optimization solution including downhole sensing , automated remote choke control, real-time water-cut measurements, the LOWIS™ life-of-well information software, and more – all integrated within the I-DO intelligent daily operation system.
Saved 16+ Hours of rig time
Compact™ microimager delivered logging data wireline-free in 6 1/8-in. hole. The tool obtained a caliper log to identify fractures in a safe, efficient operation that saved more than 16 hours of rig time.
Zero incidents 60 hours straight run time
Weatherford deployed the OverDriveTM System with the TorkDriveTM 750HD tool and ran 378 joints of casing to a 15,413-ft (4,698-m) depth – achieving one of the longest 13 5/8-in. casing runs to date.
Saved $80 million in NPT costs
The Weatherford Well Engineering and Project Management team delivered a drilling and mitigation program that safely drilled and completed sections in several wells previously deemed undrillable.