Real Results

All real results

Date Name
Mar 18
2014
Safety-Tension-Adapter System Reduces Installation Time of Drilling Blowout Preventer by Three Hours, Improves Safety

Drilling, Real Result, Weatherford World

Mar 18
2014
Capillary Injection Tubing Anchor Increases Chemical Returns, Reduces Monthly Chemical Cost by $2,800 Per Well

Production, Real Result, Unconventional, Weatherford World

Mar 18
2014
Tubing Packoffs with Gas-Lift Valves Restore Dead Well to Produce 1,000 bopd per String, Recover Investment in 1 Day

Aging Reservoirs, Conventional, Production, Real Result, Weatherford World

Feb 26
2014
Safety-Tensioning-Adapter Unit Reduces Installation and Removal Time of Blowout Preventer Systems by 17 Hours

Drilling, Real Result, Weatherford World

Feb 26
2014
Mechanized Power Tongs, HiPer™ System Integrate in Operator Equipment, Improve Efficiency, Enhance Safety in North Sea

Real Result, Tubular Running Services, Weatherford World

Feb 24
2014
RipTide® Reamer, MetalSkin® Liner Enlarge Wellbore, Isolate Water-Swellable Zone, Reach TD with Maximum Production Casing Size

Conventional, Deepwater, Drilling, Real Result, Weatherford World

Feb 24
2014
Homco® Casing Patches Isolate Highly Permeable, Underbalanced Reservoir, Enable Installation of Cemented Secondary Liner

Aging Reservoirs, Conventional, Drilling, Real Result, Weatherford World

Feb 24
2014
MetalSkin® Monobore Openhole Liner System Isolates Severe Losses in HPHT Development Well

Conventional, Deepwater, Drilling, Real Result, Weatherford World

Feb 24
2014
MetalSkin® Expandable Liner, Integrated Services Deliver Second Casing-Repair Installation in Geographically Constrained Field

Aging Reservoirs, Conventional, Drilling, Real Result, Weatherford World

Feb 24
2014
MetalSkin® Openhole Liner Isolates Depleted Zone, Maintains Maximum Hole Size, Eliminates NPT

Conventional, Deepwater, Drilling, Real Result, Weatherford World