|
Mar 03 2015
|
Renaissance® WDCL System Restores Gas Production to 3,000 m3/hr in Sour-Gas Well, Avoids Costly Workovers
Aging Reservoirs, Intervention and Abandonment, Real Result, Weatherford World
|
|
|
Mar 03 2015
|
Weatherford Thru-Tubing Services Restores Production in a Shut-In Geothermal Well
Conventional, Intervention and Abandonment, Real Result, Weatherford World
|
|
|
Feb 25 2015
|
S-88 Quenched and Tempered Sucker Rods Eliminate Interventions, Save $160,000, and Help Increase Production
Aging Reservoirs, Conventional, Production, Real Result, Unconventional, Weatherford World
|
|
|
Feb 24 2015
|
PCP Charge Pump Improves Gas Separation and Multiphase Volumetric Efficiency
Aging Reservoirs, Conventional, Production, Real Result, Unconventional, Weatherford World
|
|
|
Feb 16 2015
|
SurgeMaster™ II Tool Runs Liners Faster and Safer Than Conventional Systems and Avoids Mud Losses
Drilling, Real Result, Weatherford World
|
|
|
Feb 13 2015
|
Re-Entry Services Team Expedites Large-Bore, Dual-String Casing Exit in Remote Location and Saves Client One Day of Rig Time
Aging Reservoirs, Conventional, Intervention and Abandonment, Real Result, Weatherford World
|
|
|
Feb 04 2015
|
RapidFlo™ Plungers and Monitoring with CygNet® Software Increased Production in Declining Horizontal Gas Wells
Aging Reservoirs, Production, Real Result, Unconventional, Weatherford World
|
|
|
Jan 27 2015
|
Integrated Services Installs Record-Length Expandable Liner To Eliminate H2S Intrusion and Restore Production
Aging Reservoirs, Conventional, Real Result, Unconventional, Weatherford World
|
|
|
Jan 20 2015
|
Flexisert™ Insertable Progressing Cavity Pump Anchor Reduces Workover Cost by Nearly 80%
Aging Reservoirs, Conventional, Production, Real Result, Weatherford World
|
|
|
Jan 15 2015
|
Free-Rotating Eccentric Guide Shoe Enables TD for 400,000-lb Casing String in Extended-Reach Well, Avoids NPT
Drilling, Real Result, Weatherford World
|
|