Real Results

All real results

Date Name
Jun 20
2014
SwageSet Liner-Top Packer Provides Operator Reliable Liner-Top Isolation, Enables Production Zone to be Drilled

Drilling, Real Result, Weatherford World

Jun 20
2014
SwageSet Liner-Top Packer Used in Scab Liner Restores Well Integrity and Saves Major Operator Costs and Time

Drilling, Real Result, Weatherford World

Jun 16
2014
Weatherford Collaborative Liner System and Cementing Product Services Enable Client to Test Production Zone

Drilling, Real Result, Weatherford World

May 02
2014
DwC™ Services Save 34 Hours of Rig Time, Complete Casing Run in Single Trip

Real Result, Tubular Running Services, Weatherford World

Apr 21
2014
DwC™ Services Mitigate Drilling Hazards, Reduce NPT in Challenging Formation

Real Result, Tubular Running Services, Weatherford World

Mar 18
2014
Safety-Tension-Adapter System Reduces Installation Time of Drilling Blowout Preventer by Three Hours, Improves Safety

Drilling, Real Result, Weatherford World

Mar 18
2014
Capillary Injection Tubing Anchor Increases Chemical Returns, Reduces Monthly Chemical Cost by $2,800 Per Well

Production, Real Result, Unconventional, Weatherford World

Mar 18
2014
Tubing Packoffs with Gas-Lift Valves Restore Dead Well to Produce 1,000 bopd per String, Recover Investment in 1 Day

Aging Reservoirs, Conventional, Production, Real Result, Weatherford World

Feb 26
2014
Safety-Tensioning-Adapter Unit Reduces Installation and Removal Time of Blowout Preventer Systems by 17 Hours

Drilling, Real Result, Weatherford World

Feb 26
2014
Mechanized Power Tongs, HiPer™ System Integrate in Operator Equipment, Improve Efficiency, Enhance Safety in North Sea

Real Result, Tubular Running Services, Weatherford World