Mar 04 2024
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CalView® Tool Enhanced Operational Safety in Reentry Jobs Through Deformation Detection, Optimized Rig Time and Operational Efficiency
Formation Evaluation, Real Result, Weatherford World
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Feb 29 2024
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Capillary Injection Technology Treated Causes of Liquid Loading, Avoided Workover, Stabilized and Optimized Gas Production Without Killing Wells
Completions, Real Result, Weatherford World
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Feb 27 2024
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Successful Data Integration Enhanced Petrophysical Evaluation, Enabled Updated Reservoir Static Modeling, Revised Well Production Intervals
Formation Evaluation, Real Result, Weatherford World
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Feb 26 2024
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PressurePro® Set-Point Choke System Maintained CBHP During MPC Operations, Enabled Drilling of Two Geological Units in One Hole Section
Drilling, Real Result, Weatherford World
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Feb 26 2024
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PressurePro® Set Point Choke, MPD Technology Drilled 2 Hole Sections to TD in Longest Horizontal, Extended-Reach Well in Kazakhstan
Drilling, Real Result, Weatherford World
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Feb 22 2024
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Magnus® RSS, LWD Technology Maintained Trajectory in Deep Onshore HPHT Well, Saved 11 Days of Rig Time, Approximately $700,000 USD
Drilling, Real Result, Weatherford World
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Feb 12 2024
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RipTide® Ball-Drop Reamer, Magnus® RSS Enlarged 14 1/2 x 16-in. Section in a Single Run, Eliminated Invisible Lost Time, Set Field Record
Drilling, Real Result, Weatherford World
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Feb 09 2024
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Annular Flow Configuration of Onshore Gas-Lift System for Unconventional Well Increased Production, Reduced Workover Costs, OPEX
Production, Real Result, Weatherford World
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Feb 02 2024
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MPD Techniques, Victus™ System Thoroughly Characterized HPHT Reservoir, Eliminated Contingency Liner, Optimized Future Drilling
Drilling, Real Result, Weatherford World
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Feb 02 2024
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CalView® Tool, Interpretation and Evaluation Services Determined Accurate Measurements for Different Casing Weights of 50-Year-Old Well in Iraq
Formation Evaluation, Real Result, Weatherford World
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