Real Results

All real results

Date Name
Sep 18
2020
Victus™Intelligent MPD Solution Delivers Infill Well Through Severely Depleted Reservoir, Cuts 25 Days Off AFE Budget for North Sea Operator

Drilling, Real Result, Weatherford World

Sep 18
2020
Liner Wiper Plug Modifications Shorten Drillout Time to Save Three Hours of Valuable Rig Time

Drilling, Real Result, Weatherford World

Sep 18
2020
DiamondBack Reamer and VariForm® Centralizers Enable Setting of 7-in. Liner Through Weak Formation to Save Millions in a Challenging North Sea Well

Completions, Real Result, Weatherford World

Sep 11
2020
Magnus® Rotary Steerable System Drills 8 1/2-In. Section in 1 Run, Increases ROP by 50%, and Saves 2.8 Days of Rig Time

Drilling, Real Result, Weatherford World

Aug 10
2020
Magnus® RSS Drills Large Diameter Curve Section in an Offshore Application to Achieve All Well Objectives

Drilling, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Solution Informs Reservoir Strategy with Real-Time Flow Data, Saves $10M in CAPEX and $1.5M Annually in OPEX

Completions, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Provides Real-Time Monitoring, Optimization, and Daily Allocation for 37 Offshore Well

Completions, Conventional, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Optimizes Paired Coal Seam Gas Well Production, Reduces Dewatering Rate by 50 Percent

Completions, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Eliminates Failures in 7 HPHT, Deepwater Wells, Provides 6 Years’ Reliable Service and Provides 6 Years’ Reliable Service and Counting

Completions, Conventional, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Eliminated Electronic-Sensor Failures and Delivered Reliable and Stable Reservoir Data

Completions, Conventional, Real Result, Weatherford World