Real Results

All real results

Date Name
Aug 10
2020
Magnus® RSS Drills Large Diameter Curve Section in an Offshore Application to Achieve All Well Objectives

Drilling, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Solution Informs Reservoir Strategy with Real-Time Flow Data, Saves $10M in CAPEX and $1.5M Annually in OPEX

Completions, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Provides Real-Time Monitoring, Optimization, and Daily Allocation for 37 Offshore Well

Completions, Conventional, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Optimizes Paired Coal Seam Gas Well Production, Reduces Dewatering Rate by 50 Percent

Completions, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Eliminates Failures in 7 HPHT, Deepwater Wells, Provides 6 Years’ Reliable Service and Provides 6 Years’ Reliable Service and Counting

Completions, Conventional, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Eliminated Electronic-Sensor Failures and Delivered Reliable and Stable Reservoir Data

Completions, Conventional, Real Result, Weatherford World

Aug 07
2020
ForeSite Sense Reservoir Monitoring Delivers 100% Reliability Over 3 Years in a Multizone HPHT Offshore Well

Completions, Conventional, Real Result, Weatherford World

Jul 09
2020
COMPLETE Team Integrates Solutions to Deliver 30 Savings for Three North Sea Platforms

Completions, Real Result, Weatherford World

Jul 01
2020
Integrated Lower Completion With SwageSet Liner System and Maxflo Screen Installation Uses Minimal Cr

Completions, Real Result, Weatherford World

Apr 15
2020
Magnus® RSS Delivers Peak Performance, Service Quality to US Operators on Deep 12 1/4-In. Sections

Drilling, Real Result, Weatherford World