Real Results

Performance By The Numbers

Smart Gas Lift

Decreases Gas Injection Volumes by up to 50%, Improves Production in a Mature Field

Objectives

  • Reduce consumption of buyback gas for gas lift operations in a mature field with 150 wells in South Texas.
  • Optimize injection rates for an intermittent gas lift system.
  • Maintain or increase fluid production.
  • Keep expenditures to an absolute minimum.

Our Approach

  • Weatherford artificial-lift engineers used proprietary production optimization programs to assess production rates, gas-to-liquid ratios, and artificial lift systems throughout the field.
  • Weatherford recommended the Smart Gas Lift solution—including the WellPilot® controller—as a rigless, low-cost solution that continually calculates and injects gas to deliver the optimal amounts to each well.
  • They implemented intermittent gas lift without changing existing continuous-lift valves. The Weatherford WellPilot controller monitored casing and tubing pressure.
  • The controller also regulated and recorded gas inflow and outflow.

Value to Customer

  • The Weatherford Smart Gas Lift solution with the WellPilot controller enabled the operator to decrease gas injection volumes by up to 50% in each well.
  • WellPilot monitoring and reporting enabled the operator to concentrate oversight and maintenance only on wells showing signs of impending problems and reduce lifting costs by up to 50%.
  • The WellPilot controller maintained or increased production in the majority of wells, and the operator realized a return on investment in one to three months per well.
  • Minimal installation expenditures were quickly repaid through savings in OPEX and increases in production.
Details

Location

South Texas

Well Type

Onshore, oil and gas

Depth

10,000 ft (3,048 m)

Products/Services

WellPilot controller

Contact Weatherford

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